• Steel Soldiers now has a few new forums, read more about it at: New Munitions Forums!

  • Microsoft MSN, Live, Hotmail, Outlook email users may not be receiving emails. We are working to resolve this issue. Please add support@steelsoldiers.com to your trusted contacts.

 

pinion seal

Varyag

Member
927
2
16
Location
Garfield, Washington
Any tips on getting the castle nut off the pinion? I swear they welded that thing on.

Shouting obscenities at it doesn't appear to work either.
 
Last edited:

cattlerepairman

Well-known member
Steel Soldiers Supporter
3,173
3,095
113
Location
NORTH (Canada)
You pulled the cotter pin that locks it? Not meant to be a ridiculous question. Sometimes the cotter pin is broken off, but the remains are still in the hole, sticking out enough to lock the nut.

From then on, the usual. Soak in creeping oil of your choice. Some swear by ATF, others by AeroKroil or WD40. Soak, soak again and be patient. As in a day patient. Then tighten the nut before trying to loosen it. Then use an air gun.

It will spin off eventually. Swearing and shouting obscenities is optional but there is empiric evidence to show that it does help with stubborn tasks.
 

Varyag

Member
927
2
16
Location
Garfield, Washington
The cotter pin came out fine... and I have it setting bathed in deep creep for the moment. I have the truck super-chocked and it was moving with me trying to get it off. It laughed at my impact too.

BTW, clean your vents... I did it not too long ago and they were stuck solid again. The center axle had pressure in it when I popped it off. PNW winters are hard on these things. I am guessing it had a hand in my current seal issues.
 

scoutmanadam

New member
397
4
0
Location
richland, washington
i just removed one the other day. i had my brother hold the flange with a 18 inch pipe wrench with a cheater and i used a 3/4 inch breaker bar with a cheater and still just got it.
 

Varyag

Member
927
2
16
Location
Garfield, Washington
Yeah, I am trying to figure out how to steady the flange solo. I think I am going to take the advise to just let it soak a couple days and do other stuff I need to finish on it.

Time to inspect the front end.
 

wsucougarx

Well-known member
6,951
65
48
Location
Washington State
I got my stuck bolt off by putting a socket on the bolt and out an ext on my breaker bar. I then drove the truck s couple inches to break the thread;) Dont remember if I went forward or backwards..lol
 

clinto

Moderator, wonderful human being & practicing Deuc
Staff member
Administrator
Super Moderator
Steel Soldiers Supporter
Supporting Vendor
12,596
1,123
113
Location
Athens, Ga.
My IR 2131 and my 3/4" both got the job done.

Get a bigger badder impact. :D
 

Hottrodd789

New member
78
0
0
Location
Orlando fl
I used a snapon cordless impact with a shallow soccket cam right of no problems I also sell those impacts and a seal removal tool that makes it easy to remove seal
 

Varyag

Member
927
2
16
Location
Garfield, Washington
Unfortunatly the nut is the one between the center axle and the TC. So no moving under its own power. I am not sure I would want to drag it with the 1009 ether. I am patient and will let the deep creep do its job. I need a bigger impact too but I am worried about what a stronger tool will do to the gears that pinion is attached to if I really dug into it.
 

Josh

Active member
1,678
11
38
Location
Portland, Oregon
Unfortunatly the nut is the one between the center axle and the TC. So no moving under its own power. I am not sure I would want to drag it with the 1009 ether. I am patient and will let the deep creep do its job. I need a bigger impact too but I am worried about what a stronger tool will do to the gears that pinion is attached to if I really dug into it.
Cant ya just lock in the front wheels?.
 

gringeltaube

Staff Member
Super Moderator
Moderator
Steel Soldiers Supporter
6,882
2,259
113
Location
Montevideo/Uruguay
...... I need a bigger impact too but I am worried about what a stronger tool will do to the gears that pinion is attached to if I really dug into it.
No need for IMPACT here...
All you have to do is find/build something like a 3' long bar, possibly 1-1/2"x 5/8" or 2"x1/2" flat stock, at least on one end, then drill two 13.5mm holes in it at 78mm C-C distance and offset to one side to leave space for your 1-1/2" socket. Firmly bolt this end against the companion flange and get the other end to resting against the (drivers side)frame while applying torque with a good 3/4" breaker bar. Have the breaker bar working horizontally & lifting up assisted with a floor jack.

Always works!;-)

G.
 

doghead

4 Star General /Moderator
Staff member
Super Moderator
Steel Soldiers Supporter
26,247
1,168
113
Location
NY
I like the bar idea.

I had one that was difficult and I used a 3/8 chain bolted to one hole on the flange, then wrapped the other end around the frame. I pulled it tight enough to use the chain to keep it from rotating. I was alone or I would have just asked someone to step on the brakes.

The bar would reduce the stress on the flange.
 

DodgerRoger

Member
Steel Soldiers Supporter
32
0
6
Location
Owasso/Ok
I second the heat method, and the oil. Impact wrench, cheater pipe or whatever else doesn't really matter. I use an impact most of the time unless I have to use a really thin walled socket. If you can get the nut glowing it will probly come off. If the nut is severly rusted or the threads were buggered up when it was installed it may not come off at all without ruining whatever threads are left, in these cases cut the nut off with a torch if your good enough or find someone who is to do it for you.
 

cmpman

Member
85
7
8
Location
Manitoba Canada
Gringeltaube has it right, you need to hold the flange. I just went through this job a week ago, and fortunately I have the right tool. Kent-Moore has a flange holding tool that bolts onto the flange with a hole in the center for the socket to go through. The tool is about 3 feet long. I like to set it against either the ground or the frame.

Nice thing about the tool is it also has a second part that allows you to use it as a puller to remove the flange. The tool number is Kent Moore J-08614-a. If you search the internet for that part number or simply J8614 you should be able to find a used one for a reasonable price.

Once the flange is held solid, I used a long 3/4 powerbar to remove the nut.

The holding tool is also ideal to get the appropriate torque back onto the flange nut. While not so critical on these Rockwell differentials, it is crucial on many of the DANA differentials where the bearing preload is set by the appropriate torque.
 

Attachments

Last edited:
Top
AdBlock Detected

We get it, advertisements are annoying!

Sure, ad-blocking software does a great job at blocking ads, but it also blocks useful features of our website like our supporting vendors. Their ads help keep Steel Soldiers going. Please consider disabling your ad blockers for the site. Thanks!

I've Disabled AdBlock
No Thanks