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Thanks Coug, I appreciate the response. That's around where I was thinking. I had 12k in my head. It's a 4 man with a Maryland title. Replaced balancer and seal. New glowplugs and 1 half shaft. Also has a Tach and aftermarket alternator.
Hi all. I have a 1991 M998 and im trying to get an idea of what its worth. Its a 6.2 with a 3 speed. Plain jane, no extras to speak of. 100% operational with exception a small leak at the rear dif. I see them selling at auction for around 6-8k and some on craigslist for 20k and up. Does anyone...
Pretty simple. The only issues were getting the belt/pulley to line up and kicking the bottom of the alternator out so it doesn't hit the oem bracket. I've seen other write ups where they cut the bracket to make it fit, but I didn't want to do that. The last picture is from the m35a2 just to...
I had 40 nd in my last deuce for a month or so. It shifted fine but when I went to 90w mineral gear oil it felt like the gears were a little more cushioned if that makes sense. I could feel the gears less through the shifter. Just my observation.
I have done all 4 rear hubs over the span of a few months due to leaks. The first one I replaced the cork and both seals, the rest just got the cork replaced. Upon inspection it looks like the cork is the main culprit. Also if your bearing nut is too loose it could also cause a leak. As for...
It depends how mechanical you are. If you plan on driving it on the road you need to fix the brakes. The rears should lock up on a dirt road with not too much effort. Good luck.
I had loose u joint drive shaft bolts on both m35a2's and loose half shaft bolts on my m998. Definitely good advice to do a complete inspection before you go haulin down the road.
Changed my fuel filters for the first time in 22 years if I’m reading the date code correctly. Funny thing is that it ran good before the change. The only difference I notice is a higher idle, little higher egts, and maybe a little more power. Sounds better too.