I followed a lot of the pointers others gave here about closely looking at the pictures for hints of problems, scavaging, incomplete repairs, exhaust flap etc.
I won a unit during the 3/17 auction at Ft Meade. Drove down & picked it up on 3/24.
Engine was dry with no water in the cylinders or crankcase. Turned over smoothly by hand.
Included unused aux fuel hose with adapters, TM users manual & lubrication order.
Issues found:
- Missing 1 battery tie down rod. No biggie.
- Broken Master Switch, knew that when I bid on it. Ordered the one from Ebay, dropped it in, perfect fit.
- Radiator petcock broken off the radiator. Fixed by soldering a copper patch over the hole.
Put in 3 new Wix filters, fresh fuel, coolant, engine oil and a pair of new group 51 batteries.
Cross fingers and started to crank it. Found two fuel leaks.

One injector return hose was cracked right where it makes the tight bend from the injector to the return rail. Second leak was the fuel return hose to the tank. It was cracked where it is attached to the return fitting on the tank. Both easy fix's.
Crossed fingers a second time and cranked it again. Presto it sprang to life and runs beautifully.

Adjusted the frequency and verified the output voltages. All gauges and controls work perfectly!